Saturday 10 August 2013

Spitfire

Seen at Fairford and (possibly) Cassiobury Park on 20th/21st July was this MkXVI Spitfire from the Battle of Britain Memorial Flight, here in commemoration of 617 Sqn. Dambusters 70th anniversary.



Also from 617 Sqn...

Panavia Tornado

Saturday 13 July 2013

It's now an ornament.

Yes, sadly the KT120fsT has died. During yesterday's testing at near full throttle there was a sudden loud clatter shortly ending in silence.

Another broken crankshaft
Testing was going really well, RPM was up to 6400 at maximum throttle and idle was around 1800 on a 16 x 8 prop. The cool cylinder was beginning to heat up as running in increased the seal in the combustion chamber, although idle to full power was slow. The new carburettors were performing well after their modifications and I think further improvement could have been made to the mixture control by increasing the diameter of the air bleed into the barrel at the tick-over position. Oh! well, maybe another day, in the meantime I'll reconstruct the engine and it'll take pride of place on the mantelpiece. (As a reminder to me not to do it again).

Monday 1 July 2013

Too much noise again

Well, It seems we have someone who wants to be rid of the Flying Club at Westonzoyland. However this came in from the local Environment Officer:-

"I am writing to confirm the findings after the site visit made by myself and Mr Coles on May 31st. On that date (between 11:15 to 12:45) several model aircraft were witnessed flying including ones powered by propeller and by jet engine.
Currently based on the noise witnessed at the time of our visit there is insufficient evidence to demonstrate that a statutory nuisance exists and I have advised the complainant of this.
On the day of our site visit some planes were witnessed coming close to the no fly zone, however we were later informed that this was to demonstrate the noise at the closest point. As this latest complaint seems to have allegedly been caused by one of the propeller powered aircraft flying into the no fly zone could I therefore request that club members are reminded of this zoning.
As discussed at the time of our visit we will continue to investigate this issue if we get further complaints and where necessary liaise with yourselves to resolve any issues that may arise.
Thank you for your continued cooperation on this matter."

Problem solved? Let's hope so.

Sunday 30 June 2013

Success - allbeit limited.

I'm still struggling with the carburetor and the design in the previous blog won't do. The bends in the pipework from the carburetor to the cylinder heads are too tight and it's not possible to make them. So this time I've gone for twin carbs and they each attach directly to the cylinder heads.


It works! That propeller is an 16 x 8 Master Airscrew

After a lot of thinking and research on the internet I thought that the fuel was not burning correctly. I've put it down to the glow plugs not protruding far enough into the combustion chamber so I've made the plug recess 2.3mm deeper on the outside.

Seems to be more reliable and controllable with two carbs.

There is still some work to be done, it won't run to full power, it seems to lean out so I think perhaps I need to enlarge the fuel passages in the carburetors. This was probably the cause of the tightening that occurred at half throttle where the air flow increased and the fuel flow stayed the same. The result was a hotter burn and swelling of the pistons and creating more friction = more heat = more swelling = more friction = more heat. You can see where I'm going with this. I closed the throttle at this point and the engine stopped abruptly. I turned it over by hand and it was tight so I let it cool down and it became free again. If I can cure the the fuel starvation I think the overheating problem will be solved. I'm pleased with today's testing, a good result.

Too much noise

I visited Westonzoyland Airfield on 20th April and took my Pico-Jet and Yak 54 to fly. Just before lunchtime one of our club members left but came back a few minutes later to explain that he'd been confronted by a local resident on the subject of noise. It seems very large aeroplanes are flying very close to a residential area disturbing the occupants. (Note the word "Model" is absent).
WATCH THIS SPACE!

Monday 30 July 2012

Well, I haven't blogged here for a while...

...so here we go!
The engine you can see in the header photo has been causing me to think and the only way I'm going to get over its problem is to make my own carburettor. I've designed and manufactured a twin choke type to feed each cylinder individually. I had thought about a Plenum chamber, but the mixture will still be the same ratio for both cylinders ie. too rich for one and too lean for the other. Hopefully this will be the solution.
View on top/front
It'll fit onto the back of the engine mount, on top of the engine, hence the lug at the bottom.

Monday 5 September 2011

Hey Presto...

...Two new valves and seats. I was able to use the existing valves and cut them dowm from 14mm dia. to 11mm dia. I couldn't resist keeping the inlet valves bigger, so they're only 1mm bigger than the exhaust.


Smaller inlet valves and new seats

Sorry about the poor quality of the photo, it was taken under poor lighting conditions with my iPhone.
Next is assembly and test. This will probably take place at the weekend.

Saturday 27 August 2011

Better, but with the same old same old.

I've fired it up again and its still not performing correctly. Its better, but not right. I fear the crank shaft is suffering again. I'm going to look at the cylinder heads next and perhaps make two new inlet valves and seats. I'm thinking it was a mistake to make the inlet valves so big, so I'm going to reduce their size. Too much mixture is getting into the combustion chamber and ignition is taking place far too advanced of TDC. Its OK lower down the rev range, but when the throttle is opened it tends to labour and get extremely hot.

Sunday 14 August 2011

Back together again.

It's good to see it all in one piece. Assembly is by no means straight forward, and takes a considerable amount of care and patience. One of the trickiest parts is fitting the gudgeon pins. There is a PTFE pad on each end of the pins and you have to be careful not to push the first pad out of the other side of the piston. This is especially tricky when fitting the second pad as there isn't much space for them to fit between the ends of the pin and the cylinder bore.


Reassembled and...


...rarein' to go!

Another issue is the valve timing. The gears are cross helical and you have to "aim" the camshaft as you fit it because the working position is a few degrees away from where you first insert it due to the helix in the gears. I think I've got it right, but only testing will tell. I may have to advance or retard it a notch.

Monday 18 July 2011

All the machining is finished - I think!

It all just requires assembling. Easier said than done. Two new cylinders have been made with a thicker lip at the top to reduce the compression ratio. Made from Meehanite it is difficult to obtain a good finish in the bore so hand finishing with fine abrasive paper is required. 
Cylinder and Piston


Finished crankshaft

I finished the crankshaft today, faced off the front end and drilled and tapped the M6 thread. Next is to start the assembly. First the primary cross helical gear has to be pressed on the rear shaft. Then the inner bearings pressed on each end, and then offered into the crank case where the conrods will be fitted.

More later, I now have a job to do for a client.

Friday 15 July 2011

A new angle

Just thought I'd take some more pictures while I had the crankshaft set up to machine the counterbalance weights - in case I need to jog my memory in the future.

Two done - One and a bit to go.


Angled faces are machined at 38 degrees.

Almost finished, all that's left to do is face off the front and drill and tap the M6 thread.

Saturday 9 July 2011

Finally, a new crankshaft.

I got some infoozyazm together this weekend and have made a new crankshaft. Its not finished yet but is well on its way. To my amazement it runs perfectly true and is better than the last one. I'm going to counterbalance it this time, not as much as a single cylinder engine would be, but a bit more than "balanced".

The new crankshaft

The other thing I have to do is make two new cylinder sleeves. The originals were creating too much compression and that is what I believe was contributary to the demise of the crankshaft. I've bought some Meehanite a dense cast iron which is wear and heat resistant. I need to increase the lip thickness to raise the cylinder heads and reduce the compression ratio. The only control I have over the point of ignition is by the compression ratio. Too much and pre-ignition reduces power, increases temperature and leads to component failure as I've experienced. Too little and the engine is difficult to start, runs poorly and wastes fuel. I'll increase the lip thickness by a millimetre, if it proves to be too much I can easily remove some of the material to increase compression again.

Sunday 10 April 2011

The best day for flying.

Wall to wall sunshine and light variable winds mainly from the North made today the best by far for flying this year.
Seen at Westonzoyland today:-




BAe Hawk - Nice!

We held two competitions today, the first in the morning was a fly for fun where we had to do various events, spot landing, consecutive loops, limbo circuits and touch and goes. Planned so that it can all be done in one flight. The second was a scale competition where anything resembling a scale aircraft could enter. We had to create a flight schedule which replicated the full size. I'm glad I took the Yak, but I found it a bit challenging yet enjoyable. There were two rounds and after the first round we were shown how its done by an expert accompanied by a judge/commentator who talked us through the schedule. Then we had the second round to see if there were any improvements over the first round. I failed miserably as my Yak had an engine cut for no apparent reason and I had to land prematurely. I was allowed to restart the engine, which it did instantly, (je ne se quoi?) and continue my flight. I know I didn't do so well in the second flight as I was trying too hard, my brain kept getting in the way. Won't know the results until the AGM in December.

Saturday 5 March 2011

I've made a start.

Here we go, a new piece of stock EN16T sawn off and a flat milled all down the side. This is the location face for aligning the three centre drilled holes in each end. Once that is done it can be set up between centres in the lathe. Held in a carrier, and driven by a face plate and dog the offset journals can be machined. Here's how:-

Flat and three centres detail



Shaft held between centres



First finished journal

Saturday 19 February 2011

Disaster has struck!

After making some improvements to the Ketro 120fst I tested it today and the one piece crankshaft is now a two piece crankshaft. I am amazed the whole engine didn't smash to pieces judging by the noise it made when it let go. Fortunately there is little other damage. However, I've had some thoughts. (Careful). When the throttle opens the revs increase as expected up to a point when there is a change in the sound in that the engine sounds like its suddenly working harder yet not increasing revs any further. Open the throttle more and the revs actually decrease, yet it sounds like its working even harder. Eventually the engine cuts and has become overheated. The problems are three fold:-
  • (1) I think this problem lies mainly in the size of the inlet valve, I have designed it too big and too much mixture is getting into the cylinders and compression reaches the point of ignition too soon before top dead centre (TDC). If it were a spark ignition engine I could control the point at which ignition takes place, but this is a glow plug engine or semi-diesel and ignition is controlled by the amount of compression. I fitted restrictors in the cylinder heads to reduce the gas flow into the combustion chamber. This has helped but there are other things to be done. I may have to look at the valve timing.
  • (2) I was hoping the crank case would breathe through the front bearing and to some extent it does, but its not enough so I've incorporated a breather nipple to replace one of the gearbox retaining screws. I had to drill the existing tapped hole in the crank case through to allow the pressure to release.
  • (3) The new crankshaft I'm going to build will have a sliding fit on the rear bearings to allow for the differing rates at which aluminium (crank case) and steel (crank shaft) expand and contract with temperature change. I think the existing set-up was trying to keep things a bit too rigid and bending of the crankshaft was taking place under high temperature resulting in an annular crack in the front crank journal, and eventually leading to its failure.

The picture says it all.


Crack detail.

You can see where the crack started to form around the outside and worked its way to the centre. Click on the photo and it should enlarge.

My first job is to retrieve the gear and bearing from the rear part of the shaft. Its probably best to drill the shaft out of the gear and do the same for the bearing. It's a good thing I've got plenty of stock material left over.


Sunday 24 October 2010

I've been busy...

...Which is why I've not blogged for a while. Having just done fourteen consecutive days at work other things have gone by the bye. BUT I've finished Jims undercarriage job and is awaiting delivery.


Jims new undercarriage part

Saturday 28 August 2010

A job for Jim

I've been challenged with this job for Jim. I've made a start...



A broken undercarriage pivot


A new part in the process


Sunday 22 August 2010

A fine days' flying

The forecast for today has looked promising for a few days and lo and behold, it was right. Almost windless for most of the day, until mid afternoon when the wind picked up from the South.

Ians F15 Eagle

Today was a near perfect day. No one had a serious accident, Jims new jet had a bit of a kangaroo landing and scratched some paint, but no serious damage, and I lost a tail wheel from the Yak, hey-ho!

I tried out my KT120fsT this evening (before it rained) and got nowhere with it, It still stops when hot, and it certainly gets hot, too hot, but the engine isn't tightening up as its free to turn over by hand immediately after stopping. There is some pre-ignition at times and I think this may be a clue to the problem. I may have to have a closer look at the valve timing, and/or place yet another gasket under the cylinder heads. Some experimentation required.

Sunday 15 August 2010

I've had it running again...!

...with more success. I turned up a pair of 0.3mm thick copper gaskets to reduce the compression ratio and tested the running characteristics again but there was still some pre-ignition going on at higher revs. Back to the machine shop then, and two more copper gaskets for reducing the compression ratio even further. Now there's hardly any pre-ignition, but I'm now finding the engine stops when it gets hot and there's hardly any compression. I know the bores were a bit rough on surface finish even after honing and this is due to the cast iron being porous. I'm tempted to make two new sleeves from a different material. That way I can build in the extra thickness required to reduce the compression ratio and do away with one gasket under each cylinder head.

Here's a short video:-

Ketro KT120fsT in action

Tuesday 10 August 2010

Cornwall was a real success

Everything fell into place, even the weather was spot on. We drove down early Friday morning in heavy cloud which turned into drizzle and fog over Bodmin Moor and although the fog cleared the drizzle remained on and off all the way to North Cliffs. We parked the caravan and put up the awning and waited for Geoff and Mary to arrive. They started out before us but didn't arrive until after 12:30. They'd been mooching around Redruth and Camborne all morning because they thought it may be muddy as well as wet up on the hill. But things didn't improve so they came up later.

On Saturday the weather changed. After an early shower it turned fine with 8 MPH winds from the West and broken sunshine all day, and Sunday was even better, 2 MPH winds also from the West, and near unbroken sunshine.

Me with Yak 54, photo courtesy of Geoff.

There were some nice aircraft to be seen at the show including a Stirling bomber, a deHavilland Mosquito and a Spitfire. A few jets put in an appearance with a Rookie, Kangaroo, Boomerang and an F16 flown very realistically by its skillful pilot. The electric slot was well over subscribed so the time allocation was doubled, electric gliders and slower craft first, followed by the faster EDF (Electric Ducted Fan) jets and other fast craft. That included me with the Pico-Jet.


A 180 panoramic

deHavilland Mosquito built and flown by Roger Kellow

Rogers Mozzie developed a problem during flight in that the undercarriage failed to lock down, but was able to recover from the situation and landed safely. Well done Roger.

Also impressive was a helicopter built by Kim Johns. Now helicopters leave me cold, I just can't get interested yet I feel compelled to watch in case it starts heading this way in an uncontrolled manner. But this was different. Modified and developed to accept a gas turbine, it was flown expertly by Mark Milne and performed just like a full sized helicopter. Even the sound and smell was the same. I'm told its the only one of its kind in the world - very impressive.

Sunday 1 August 2010

I've had it running...!

...on both cylinders! Driving a 16" x 8" Master Airscrew propeller, and its too small. I've found it labours when it gets hot, so I think the pistons may be expanding, reducing the clearance in the bore. Its not been up to maximum revs as I'm still trying to find the best carburettor settings.
I can confirm the pistons have expanded whilst hot as there are shiny areas on the sides where friction has occurred. I set them up in the lathe and machined off a minimum amount, just enough to clean the sides. The rear bearing had just started to break up, this is a very small bearing at 3mm id x 6mm od x 2.5mm tk. Part of the metal dust cage had come out and some balls were missing, so I removed the what was left and replaced it with a spare. Now in the middle of reassembly. Should have it running again soon.
Off to Cornwall this coming weekend, but I don't hold out much hope of having it ready in time. There's too much work to do on the aircraft (Ultimate Biplane).

Monday 26 July 2010

Not much left to do

Two holes to be drilled and tapped M1.6 in the bottom of each conrod and then the shells have to be made. Like the small ends, the big end shells are made from Phosphor Bronze. Two flat pieces are soft soldered together, held in a four jaw chuck and drilled (under size at this stage) on the joint. Then the outside diameter is turned to size and parted off. Warm gently to melt the solder and split the shells. Fit them in the big ends and tighten with the M1.6 screws, then set up on the mill and bore the big ends to size. Job done. Then its a matter of fitting it all together and seeing if the engine runs.

To give you an idea of the size, the distance between centres is 29.0mm.


Conrods with small end bearings fitted

Sunday 18 July 2010

Nearing completion, but its a lot of tedius work

The crank shaft is almost finished, its been hard work as only small cuts at a time can be taken so as not to strain the setting. Its only held between centres in the lathe and if a tool were to pick up it would be disaster. As it is I'm very pleased with it. I need to reduce the weight a little and I've been studying some pictures of the Saito twin cylinder crank shafts and the balance weights have been shaped as a semi diamond on both sides ie where the counter balance weight would be. So I'm going to do the same.




You can see what I mean by the diamond shape...

I need to cut the same on the other side.

Monday 12 July 2010

A Jet event at Westonzoyland

This was by invitation only and some pilots from the South East area Arrived on site for the weekend to "have a go" at flying from tarmac for a change. Everyone enjoyed themselves and there were no accidents or incidents. Normal Club flying activities continued as usual and the whole event went very well.



Friday 9 July 2010

Some engineering at last

I've shelved the earlier crank shaft and decided to manufacture it a different way. This is how its done... a picture paints a thousand words, so here's a video.

Sunday 20 June 2010

Spent the day flying

A cold wind from the North but it slowly warmed up as the day went on. The wind increased in strength and became gusty making flying conditions difficult as landings had to be cross wind. Just after 13:30hrs and I was the only one there after a good crowd earlier. Jim and Ian turned up with their jets later and the wind calmed a little and direction changed to the North West.







I really must get on and do some engineering...

Thursday 13 May 2010

Thats it for a while!

I case you're wondering what been happening, I've been doing this!

Saturday 24 April 2010

Another Crankshaft Failure

Yes, it failed again. This time it twisted slightly which meant the pistons didn't reach top dead centre at the same time, and the central crank web was rotating eccentrically in the crank case. This also meant the valve timing had slipped and the pistons were just hitting the valves of one cylinder. Luckily no damage was done, and now I've decided to manufacture a one piece crankshaft and the material arrived this week. Its a good job I made the crank case with a bulge in both sides as I'm going to need that internal volume for the much larger two-part big ends of the conrods. The material is an alloy steel, EN16T which is a tough steel, good with torsional strength. The down side of all this is that (as I mentioned earlier) I have to make two new conrods with a split big end and a split bearing. This bearing is made by soft soldering two pieces of phosphor bronze together and turning the bearing as one piece, then heating it up to melt the solder to form the two big end shells.
To give you an idea of the size, the cutter in the photo is 6.0mm diameter.

Crankshaft during remanufacture


Saturday 10 April 2010

Best day for flying so far this year

Wall to wall hazy sunshine and light winds from the East. I thought it best to go today as the weather for tomorrow (Sunday) is breezy. Took the Pico-Jet, Sunbeam and the Yak and actually plucked up the courage to fly it. Had an engine cut shortly after take off, despite extensive pre-flight testing. The next flight was OK, but I had to stop to video this:-

Ians F16 is always an impressive display.

Two flights with each aircraft today, and I brought them all home in one piece - a very satisfying day.

Thursday 1 April 2010

No April Fool

So this blog is about yesterday. (Wednesday 31st March 2010).


I've managed to re-assemble the KT120fsT and fit it to the fuselage of the Ultimate. I packed it all into the car and took it to work because at 19:00hrs the factory hooter goes off and I shout "Yaba Daba Doo"! (Flintstones connection) and then its time for a quick sprint over to the George Inn at Middlezoy to enter the Sedgemoor Clubs' Craftmans Cup. This is a chance to see what club members get up to in the cold dark Winter months.


A fine array of models had been built among them an Augusta helicopter, a Hawker Typhoon, a Corsair, and a Kyten. All very nicely finished, and of course its good to get together and have a natter.

2010 to be engraved

The Craftmans Cup 2007
Ketro KT54fs




The Craftmans Cup 2010
Ketro KT120fsT

Right! Whats next? How about a KTxxxfs7R? Hmmm, maybe??? What do you think?